[1]許曉明.進水以高濃度工業(yè)廢水為主的污水處理廠擴建工程設(shè)計[J].中國給水排水,2021,37(4):71-75.
XU Xiao-ming.Design of Expansion Project of a WWTP with Industrial Wastewater as the Main Feed Water[J].China Water & Wastewater,2021,37(4):71-75.
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XU Xiao-ming.Design of Expansion Project of a WWTP with Industrial Wastewater as the Main Feed Water[J].China Water & Wastewater,2021,37(4):71-75.
進水以高濃度工業(yè)廢水為主的污水處理廠擴建工程設(shè)計
中國給水排水[ISSN:1000-4062/CN:12-1073/TU] 卷: 第37卷 期數(shù): 2021年第4期 頁碼: 71-75 欄目: 出版日期: 2021-02-17
- Title:
- Design of Expansion Project of a WWTP with Industrial Wastewater as the Main Feed Water
摘要:- 浙江某污水廠進水中含有70%的工業(yè)廢水,具有有機物濃度高、沖擊負荷大、乳化油濃度較高的水質(zhì)特點,且出水水質(zhì)要達到《城鎮(zhèn)污水處理廠污染物排放標準》(GB 18918—2002)中一級A標準。已建一期工程(2×104 m3/d)采用AAO+高效沉淀池+濾布濾池工藝處理污水,出水有機物超標嚴重。為此,二期擴建工程(2×104 m3/d)采用調(diào)節(jié)池+混凝氣浮組合池+A/O生化池+高效沉淀池的工藝流程。設(shè)計中增設(shè)調(diào)節(jié)池調(diào)節(jié)進水水質(zhì)水量;采用混凝氣浮組合池去除進水中的乳化油,以避免對后續(xù)工藝運行造成干擾;延長生化池停留時間,強化對有機物的去除,避免在深度處理階段設(shè)置高級氧化工藝,節(jié)省建設(shè)、運行費用;氣浮污泥采用離心脫水,生物污泥采用帶式脫水機處理。工程試運行期間出水水質(zhì)穩(wěn)定達到設(shè)計標準,直接運行成本為0.56元/m3。
Abstract:- The influent of a wastewater treatment plant in Zhejiang Province contained 70% industrial wastewater with high concentration of organic matter and emulsified oil, as well as high impact load. However, the effluent should reach the first level A criteria specified in the Discharge Standard of Pollutants for Municipal Wastewater Treatment Plant (GB 18918-2002). AAO tank, high-efficiency sedimentation tank and cloth-media filter were used in the first-stage project(2×104 m3/d), which caused severe excess of effluent organic matter. Therefore, the regulating tank, coagulation/air floatation unit, A/O tank and high efficiency sedimentation tank were applied in the second-phase expansion project (2×104 m3/d). The design features were as follows: adjusting the quality and quantity of influent by adding a regulating tank; The coagulation/air floatation tank was used to remove the emulsified oil, so as to avoid the interference with the subsequent process operation; By extending the residence time of the biochemical tank, the removal of organic matter was strengthened, advanced oxidation process could be avoided in advanced treatment stage, which would save the costs of construction and operating. For air floatation sludge, centrifugal dewatering were selected, and belt filter dewatering were selected for the biochemical sludge. During the trial operation of the project, the effluent quality was stable and reached the design standard, and the direct operation cost was 0.56 yuan/m3.
相似文獻/References:
[1]尹海龍,廉勍.生活和工業(yè)融合區(qū)污水處理廠運行評估分析[J].中國給水排水,2020,36(21):87.
YIN Hai-long,LIAN Qing.Evaluation and Analysis of Wastewater Treatment Plant Operation in Residential and Industrial Hybrid Areas[J].China Water & Wastewater,2020,36(4):87.
[2]尹真真,趙麗,范圍,等.城市生活污水廠處理工業(yè)廢水的運營管理對策[J].中國給水排水,2020,36(24):54.
YIN Zhen-zhen,ZHAO Li,FAN Wei,et al.Suggestions on Operation and Management of Urban Domestic Sewage Treatment Plant Handled Industrial Wastewater[J].China Water & Wastewater,2020,36(4):54.
更新日期/Last Update: 2021-02-17